HBF comes out of retirement

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Re: HBF comes out of retirement

ArdWrknTrk
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I'm glad no one was hurt.
Thoughts of early cell phone reception remind me just how much our lives have changed.

Just a few months ago I had to rebuild my tire carrier.
It's beefier now.
No matter if you flush the undercarriage any time the hose isn't frozen the road salt in the north eats everything up.
 Jim,
Lil'Red is a '87 F250 HD, 4.10's, 1356 4x4, Zf-5, 3G, PMGR, Saginaw PS, desmogged with a Holley 80508 and Performer intake.
Too much other stuff to mention.
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Re: HBF comes out of retirement

HBF84
Well, I gave my gas filler hose another try at the old hack routine and it seemed to have worked for at least two full tanks of gas now.  So, I might just return the brand new hose.  Posting this for anyone in a similar situation but no promises it will work long-term!

I found a piece of radiator hose about 4 inches long and sliced it lengthwise.  Then, I sanded my filler hose that was dry rotted and caked with dirt and grime.  The filler hose was leaking each time I filled up the tank and there was a noticeable small hole.  To the inside of the radiator hose, I applied some pipe joint compound that said on the back that it could be used with gas.  (I suspect the meaning was for natural gas pipes/propane lines but hey, I had been given a few bottles of it, and figured it was worth a try!)  Then, slipped the radiator hose on the filler hose.  And then gently tightened some hose clamps around the two hoses.  So far, so good!



1984 F-150 2wd short bed with 4.9L, 4 speed overdrive manual transmission, and 3.08 rear end (18) switched to the 3.55 limited slip (H9).
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Re: HBF comes out of retirement

Gary Lewis
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Well, if it works...  This document says "fuel lines" and I would think that would include gasoline.  So I think you are ok.

Keep us posted, please.
Gary, AKA "Gary fellow": Profile

Dad's: '81 F150 Ranger XLT 4x4: Down for restomod: Full-roller "stroked 351M" w/Trick Flow heads & intake, EEC-V SEFI/E4OD/3.50 gears w/Kevlar clutches
Blue: 2015 F150 Platinum 4x4 SuperCrew wearing Blue Jeans & sporting a 3.5L EB & Max Tow
Big Blue: 1985 F250HD 4x4: 460/ZF5/3.55's, D60 w/Ox locker & 10.25 Sterling/Trutrac, Blue Top & Borgeson, & EEC-V MAF/SEFI

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Re: HBF comes out of retirement

ArdWrknTrk
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In reply to this post by HBF84
I wish you luck.  

Not sure how much that hose costs.
Did you determine how it got a hole in it?
 Jim,
Lil'Red is a '87 F250 HD, 4.10's, 1356 4x4, Zf-5, 3G, PMGR, Saginaw PS, desmogged with a Holley 80508 and Performer intake.
Too much other stuff to mention.
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Re: HBF comes out of retirement

HBF84
Thanks gentlemen!

I suspect the hole was from rubbing against the frame and then dry rot over 10 years.  I am pretty confident it wasn't dribbling out when I filled up the tank last in either December 2009 or January 2010.  However, when I went to siphon the gas out in May 2020, I disconnected the metal section from the rubber section.  And, I wonder if doing so, I tore the rubber section.  So, ya know, it coulda been a combo of dry rot, the frame constantly rubbing on it, and my overaggressive inept gorilla hands.    
1984 F-150 2wd short bed with 4.9L, 4 speed overdrive manual transmission, and 3.08 rear end (18) switched to the 3.55 limited slip (H9).
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Re: HBF comes out of retirement

HBF84
Another hack I did recently... For anyone interested in the guts of the mirror:





I pealed off the glue/sticky pads and cleaned the surfaces as best as possible.  Then, the mirror was glued back to the base with some Gorilla Epoxy.  This was in May 2020 and so far so good!



1984 F-150 2wd short bed with 4.9L, 4 speed overdrive manual transmission, and 3.08 rear end (18) switched to the 3.55 limited slip (H9).
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Re: HBF comes out of retirement

ArdWrknTrk
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This post was updated on .
I usually use silicone, but if it's been holding up for seven months I'd call it good!  

Wish I could get them to *fall off in one piece instead of shattering.  
 Jim,
Lil'Red is a '87 F250 HD, 4.10's, 1356 4x4, Zf-5, 3G, PMGR, Saginaw PS, desmogged with a Holley 80508 and Performer intake.
Too much other stuff to mention.
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Re: HBF comes out of retirement

HBF84
Yes Sir, I got lucky!  The mirror was vibrating a lot and I figured it was the lower swing arm mount.  The rivet that the lower swing arm pivots on had broken many many years ago.  So, I was going to pull the whole thing assembly off and drill out the rivet and put a bolt through it.  (Which I still haven't done.)  Anyhow, as I started doing that, I realized it was the actual mirror in a tenuous position!
1984 F-150 2wd short bed with 4.9L, 4 speed overdrive manual transmission, and 3.08 rear end (18) switched to the 3.55 limited slip (H9).
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Re: HBF comes out of retirement

ArdWrknTrk
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Maybe the added vibration led to the mirror shaking loose?

I once noticed my drivers side mirror was not adjusted right.
I reached out the open window and the whole head came off in my hand!

The neck of the ball had rusted through.
 Jim,
Lil'Red is a '87 F250 HD, 4.10's, 1356 4x4, Zf-5, 3G, PMGR, Saginaw PS, desmogged with a Holley 80508 and Performer intake.
Too much other stuff to mention.
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Re: HBF comes out of retirement

HBF84
I suspect you're right!  The extra vibrations likely shook the mirror loose from the glue pads!

Another thing hanging by just a thread... My exhaust/heat shield thingy.  One bolt was still holding it on.  Where the other bolt was, the shield had rusted away around it!  And, of course, when I tried to remove the bolt, I broke the bolt and the thread is lodged in the intake manifold.  So....

Ideas on how to fix this or to find a replacement?!?  How critical is it?!?  



Today, I bought a small roll of roof flashing and have tin snips.  I also bought some aluminum foil tape while I was at the hardware store.  
1984 F-150 2wd short bed with 4.9L, 4 speed overdrive manual transmission, and 3.08 rear end (18) switched to the 3.55 limited slip (H9).
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Re: HBF comes out of retirement

ArdWrknTrk
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I didnt know these warm inlet air shrouds bolted to the intake on 4.9's
On V-8's they are held by a double sided stepped stud, so even if the shroud nut breaks off the stud holds the exhaust manifold tight.

I'm sure heated air in winter helps a 4.9 especially.
But it's absence isn't going to hurt anything.

I had to weld some stainless fender washers into mine because it had completely disappeared around the studs.
 Jim,
Lil'Red is a '87 F250 HD, 4.10's, 1356 4x4, Zf-5, 3G, PMGR, Saginaw PS, desmogged with a Holley 80508 and Performer intake.
Too much other stuff to mention.
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Re: HBF comes out of retirement

HBF84
Well, it got a bit colder this week so I figured I would try to see if the lack of the exhaust shield feeding warm air to the carburetor was the cause of the persistent high idle.  And, after a quick trip to the hardware store for some aluminum tape and flashing, I fashioned this:





It seemed to work with the temperatures in the 40's but not last night when it was about 25 or so.  

1984 F-150 2wd short bed with 4.9L, 4 speed overdrive manual transmission, and 3.08 rear end (18) switched to the 3.55 limited slip (H9).
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Re: HBF comes out of retirement

ArdWrknTrk
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It's got to be helping!    

Poor atomization and carb icing are very real.
Any warmth the inlet air sees is better than none.  
 Jim,
Lil'Red is a '87 F250 HD, 4.10's, 1356 4x4, Zf-5, 3G, PMGR, Saginaw PS, desmogged with a Holley 80508 and Performer intake.
Too much other stuff to mention.
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Re: HBF comes out of retirement

Gary Lewis
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It will help with atomization, but not the high idle.  The choke heater should be bringing the choke off, with or without heat through the air cleaner, and as the choke comes off the fast idle should drop down.  If it isn't dropping down and eventually coming completely off you need to make sure that the choke heater is working and bringing the choke off.  And if that's the case then figure out why the fast idle linkage may be stuck.
Gary, AKA "Gary fellow": Profile

Dad's: '81 F150 Ranger XLT 4x4: Down for restomod: Full-roller "stroked 351M" w/Trick Flow heads & intake, EEC-V SEFI/E4OD/3.50 gears w/Kevlar clutches
Blue: 2015 F150 Platinum 4x4 SuperCrew wearing Blue Jeans & sporting a 3.5L EB & Max Tow
Big Blue: 1985 F250HD 4x4: 460/ZF5/3.55's, D60 w/Ox locker & 10.25 Sterling/Trutrac, Blue Top & Borgeson, & EEC-V MAF/SEFI

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Re: HBF comes out of retirement

ArdWrknTrk
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Don't all the YF's have that red silicone hose coming from the choke stove?
Are only some of them electric assist?

I'm not too fluent in 4.9.  
 Jim,
Lil'Red is a '87 F250 HD, 4.10's, 1356 4x4, Zf-5, 3G, PMGR, Saginaw PS, desmogged with a Holley 80508 and Performer intake.
Too much other stuff to mention.
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Re: HBF comes out of retirement

Gary Lewis
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I don't know the answer to that question.  I don't speak YF/A very well.  Which is why I was careful to say "choke heater" as I didn't know what form it might take.

But, to me, a high idle in cold weather implies the choke isn't coming off.
Gary, AKA "Gary fellow": Profile

Dad's: '81 F150 Ranger XLT 4x4: Down for restomod: Full-roller "stroked 351M" w/Trick Flow heads & intake, EEC-V SEFI/E4OD/3.50 gears w/Kevlar clutches
Blue: 2015 F150 Platinum 4x4 SuperCrew wearing Blue Jeans & sporting a 3.5L EB & Max Tow
Big Blue: 1985 F250HD 4x4: 460/ZF5/3.55's, D60 w/Ox locker & 10.25 Sterling/Trutrac, Blue Top & Borgeson, & EEC-V MAF/SEFI

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Re: HBF comes out of retirement

FuzzFace2
Gary Lewis wrote
I don't know the answer to that question.  I don't speak YF/A very well.  Which is why I was careful to say "choke heater" as I didn't know what form it might take.

But, to me, a high idle in cold weather implies the choke isn't coming off.
I also don't know the answer to that question
I know my 81 is the asst. type but I also had to "mod" the choke hot pipe.
I am using EFI manifolds and they don't have a way to pass the tube through the manifold so I got copper tubing and made a few wraps around 1 of the manifolds.

A few weeks back I adjusted the choke as the fast idle was not coming on, think the choke was not closing enough. I now think I went to much as I stays on a little longer than I think it should.
Or did I not make enough wraps of the tubing?

I am heating the intake with a hot water plate but I don't have the hot air inlet part as there is no way to have one on the EFI manifolds. As said this hot air intake will not have anything to do with the fast idle coming off, that is a choke thing.

As for the icing of the carb.
I don't think I have had any issues with that but it is only 2 miles to the high way with 1 (1/4mile from house) maybe 2 (2 mile mark) lights and only the fist I have to stop at 99% of the time.
Other wise on the high way for 37 miles, and then 2 miles, no lights to work.
So not a lot of idle time where I think the icing would show up most of the time?

I am running the factory tear drop air filter assy. with the vacuum hose / flapper hooked up and think it works as I have not checked.
Just what I found with my set up.
Dave ----
Dave G.
81 F100 flare side 300 six / AA OD / NP435 / 2.75 gear
http://cars.grantskingdom1.com/index.php/1980-Ford-F100?page=1
81 F100 style side 300 six/SROD parts truck -RIP
http://cars.grantskingdom1.com/index.php/1981-Ford-F100
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Re: HBF comes out of retirement

ArdWrknTrk
Administrator
The point I was trying to make is that the carb is out there in the middle of an intake hanging off the side and getting no heat from the block (and in the case of EFI manifolds no heat to the floor of the plenum!)

The carb is a restriction and as the intake charge expands it uses heat. As the fuel atomizes and vaporizes it consumes heat too.
There is a large cooling effect which means condensation and puddles of fuel.

Even in Dave's case, that plate isn't warming up until the truck warms up.
It isn't helping when it's needed most.
With the factory carb setup hot exhaust gases are licking at the plenum floor from the first moment the engine fires.
Flames, as hot as it gets, are swirling around directly under the carb.

Yes, none of that affects how fast the choke warms up and comes off.
Maybe Dave needs a few more turns of the worm?
Maybe there would be better heat transfer if he brazed it directly to the E manifold casting?

Maybe it's better to ditch the choke stove and go with a full electric option from Mike's Carburetor Parts?

Like I said I'm no 4.9 expert. But cold affects all carburetor enriching circuits pretty much the same, and the faster you can get the engine up to temp and the choke off, the better.
 Jim,
Lil'Red is a '87 F250 HD, 4.10's, 1356 4x4, Zf-5, 3G, PMGR, Saginaw PS, desmogged with a Holley 80508 and Performer intake.
Too much other stuff to mention.
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Re: HBF comes out of retirement

HBF84
Thank you for the informative dialogue!  I will certainly lubricate the choke linkage before I start tearing into the carburetor!  And, it ran much better today but of course, it was a bit warmer today.  Which brings me to this...

HBF was enjoying retirement in California and is a bit perturbed that he is working here in Maryland.  So, this morning, in the garage, I started up his engine and took a look at the mixing valve.  It isn't a heated garage so the air was probably about 40 degrees.  And, I took this picture:



So, the air entering the carburetor is normal air.  I reached inside and flipped the valve so that heated air entered the carburetor.  Nothing changed and it ran well this morning.  HOWEVER, is this air diversion valve controlled by a bimetallic mechanism or is it vacuum controlled?  Does that influence the conversation above?
1984 F-150 2wd short bed with 4.9L, 4 speed overdrive manual transmission, and 3.08 rear end (18) switched to the 3.55 limited slip (H9).
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Re: HBF comes out of retirement

HBF84
And, one more thing while we're talking about air...



The vermin had made a little racetrack around the air cleaner but they never were able to break through the fence and run around on the infield!
1984 F-150 2wd short bed with 4.9L, 4 speed overdrive manual transmission, and 3.08 rear end (18) switched to the 3.55 limited slip (H9).
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